What was I thinkig?

Well I did one of those bone head things I can kick myself over it.
I went to pull my plugs this weekend for a close examination and replacement.
Using a torque wrench from Sears I stripped the threads out from the head (completely out) I should add.
Lesson learned? Always read the instructions before using a new tool.
I never heard or felt the "Click" I kept pulling! Stupid Stupid Stupid mistake.

Good news I launch a massive web exploration on this topic. What I found was a tons of useful information and tools for fixing such an issue. Man was I relieved ....

After reviewing a number of scenarios I settle on fixing the head on the engine, then remove it and clean the cylinder. This will cost me a head gasket so be it.
I know in a pinch I could have grease the tap to catch most of the metal shavings from falling into the cylinder, turn the flywheel by hand and position the piston to BDC and use compress air and blow it out the exhaust port etc.
I was going to pull the heads for a close examination of my cylinder walls anyways it was on my to do list. It just got bumped up on the list.

I have seen tools on the web starting at 40 to 300 dollars..All boasting various advantages etc...

I woke up this morning brew some coffee and decided to visit Auto Zone on a hunch looking for a special tool, low and behold I came across a economical tool for the the job. $29.99

Purchase it came home call my buddy Curt over and we went to work.

Using the tool and following the instructions we finished in less than 20 minutes re-treading the hole and installing the "insert".
I will pull the head when the gaskets arrives to fully complete the job next Saturday or during the week maybe.
Scope of work...
Rotate the flywheel by hand and position the piston to the bottom of the cylinder.
Exhaust port is now fully open not like it matters to me anyways since I am going the remove the head later.
Lube the special tap with cutting oil or grease.
Insert the tap into the hole and hand tighten, use the appropriate socket and slowly start to work the tap in using fluid motion, do not back out until the tap is completely threaded in. In the picture it was not all the way in ...

Stop use a little paint brush and clean around the outside of the tap.

Slowly back the tap out completely and set it aside you are now done re-treading the hole for the insert.

Brush out all excess metal shavings away, you now have a perfect threaded hole for the insert as shown in the picture.

Observe the correct orientation for the insert corrugated end up as per instructions.

I use permex lock-tight for the sealant, Type shown is specially design for this type of use, permanent lock if so to speak and heat tolerance to 500 degrees. Its all posted at the back of the product, many to choose from.

Use a cloth with generous amount of rubbing alcohol or acetone and clean the new treads of all the grease or oil use previously.

Use a old plug and screw on the insert all the way up on the treads of the plug. You will be using the plug the screw the insert into the head.
Lube the outside treads only with the tread locker be careful cover the treads completely but not dripping etc.
Holding the plug slowly screw the insert into the head and tighten ever so gently, Wait a few minutes and slowly remove the spark plug.

Clean up around the top of the insert of any excess tread locker.

Use the drift punch or swage tool provided with the kit and tap the insert into head gently. This is actually spreading (expanding) the insert in such a way the corrugated part into the head.
The objective here is not to have the insert unscrew on the plug during future plug changes.
Let the tread locker cure per instructions, in my case the type used called for 24 hours to a full cure. Mine will be all week since I will be removing the heads next weekend to clean up the inside.
Here are the pictures , Sorry I did not snap a picture of the stripped treads let me assured you it was all gone!
 

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Pictures ...
The last photo shown is what a normal plug treads looks like ...
 

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Really nice job nymack66. You took your time, thought things out and acted correctly. Great pics too I might add. Well done sailor. :clap::clap:
 
looks good, i worked in a lawn mower repair shop and we put in hundreds of those. we called them heli-coil kits.
 
thats what i get for being on the computer without 2x reading glasses. heli-coils look like springs, i see now they are a solid piece, almost like a threaded bushing. these actually look a little more substantial, although we never had a helicoil fail, anyway, a lot cheaper than new heads.
 
Nice repair.....thats one of those things where you first think holy crap am I screwed or what?....and then it occurs to you that you cant possibly be the only guy in the world to do it and somebody has already figured out how to fix it relatively easily.
 
Heli-coils have a special tap that has slightly elongated threads. The heli-coil itself is like a spring...it's not solid. After you thread the hole you screw the heli-coil onto a special inserter tool. When you insert the coil into the newly threaded hole the slight streach of the coil then mimics the regular tpi of the bolt hole. You have to use a special inserter (comes with the kit) to insert the heli-coil, and after it's inserted you have to use a hammer and punch to break off the inserter tang at the bottom of the thread. I've used them on hundreds of different sized holes in my day, but truthfully never did a spark plug hole with them. 5/16x18, 3/8x16 and 1/4x20 are the most common sizes used. They work well on bolts that are not removed on a regular basis.

The problem with heli-coils is that they tend to loosen up or come out with bolts that are removed over and over, so they aren't the best bet for spark plug holes where you remove the spark plug on a normal maintenance basis. For holes like that I highly recommend genuine time-serts (www.timesert.com) because they do several important things. 1) They have a shoulder on the top that provides a positive stop and prevents the insert from threading itself deeper into the hole. and 2) the last few threads of the insert are not fully finished, so that as you screw the insert into the hole the bottom threads expand, and that permanently locks the insert into the head metal.... no locktite is needed. They are a little more expensive, but in my opinion, they are well worth the extra bucks .:beer:
 
Speaking of dumb moves... I blew my engine up about two weeks ago. Tried to start it, forgetting that the the plugs were out. The fuel under the cowling caught a spark somewhere and BLAMO! Lesson learned there. The explosion separated one of the latches from the cowling (which was easily epoxied back), blowing it halfway open and starting a small fire that burned on the fuel and oil in the motor housing until extinguished. I then learned that the extinguisher on the boat had no charge and had to dash for another in the garage. Overall no damage. Just some burnt wire sleeves. The only real bummer was that some fire extinguisher discharge made it into the open cylinders. I blew them out with compressed air and cleaned it the best I could. I'm hoping that didn't or won't cause any harm.
 
Speaking of dumb moves... I blew my engine up about two weeks ago. Tried to start it, forgetting that the the plugs were out. The fuel under the cowling caught a spark somewhere and BLAMO! Lesson learned there. The explosion separated one of the latches from the cowling (which was easily epoxied back), blowing it halfway open and starting a small fire that burned on the fuel and oil in the motor housing until extinguished. I then learned that the extinguisher on the boat had no charge and had to dash for another in the garage. Overall no damage. Just some burnt wire sleeves. The only real bummer was that some fire extinguisher discharge made it into the open cylinders. I blew them out with compressed air and cleaned it the best I could. I'm hoping that didn't or won't cause any harm.

Which is exactly why you carry a Co2 extinguisher onboard your boat. No residue to clean up. I'm sorry you had the fire. Lesson learned as they say.

Because ot the EPA, tree huggers and global warming BS you can no longer buy them, but if you can find them the absolute best extinguisher to have is a Halon unit. Safe, effective and zero residue. Next best is the Co2 units, but not as safe in a confined space since the carbon dioxide displaces oxygen. Lastly is the good old dry powder that you used.. good, effective but makes a mess to cleanup afterwards.
 
Motor is back in action, I pull the heads off clean up the metal shavings, Cylinders look excellent, perfect block no corrosion ...Running her on the lake tomorrow ...
 
Thanks for asking, she ran beautiful, I am in the process of really fine tuning this engine, I also made some changes to the Jets per Firm recommendation this engine never ran so good. Sorry about your mis-hap on our motor thank God nobody got hurt.
 
Using a torque wrench from Sears I stripped the threads out from the head (completely out) I should add.
Lesson learned? Always read the instructions before using a new tool.
I never heard or felt the "Click" I kept pulling! Stupid Stupid Stupid mistake.

I've busted a bolt using a sears torque wrench even after reading the directions. Since then, I went to the type that has a pointer and gauge. Much better tool IMHO...

rkc
 
Thanks for asking, she ran beautiful, I am in the process of really fine tuning this engine, I also made some changes to the Jets per Firm recommendation this engine never ran so good. Sorry about your mis-hap on our motor thank God nobody got hurt.


Sounds like you did a great job pullin out of what started out as a nose-dive!!...way to go, Mack!!...:party:
 
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